Thread Rating:
  • 0 Vote(s) - 0 Average
  • 1
  • 2
  • 3
  • 4
  • 5
TRX 3.3 engine problems
#26
that little blue beice fell in there when i was looking......I blew it off
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#27
I think it sucked in some dirt through the exhaust system.....cause there are scratches on the bottom of the connecting rod and a small gouge in the piston......i always hade the air filter on there....the only way it could have gotten dirt in is becuase of the o.s. header, cause before i bought a some rubber things for the o.s. header to fit it wasnt making a seal.....so dirt must have gotten through there becuase i couldnt even shut the engine off with my finger on the exhaust, it would just keep running......

so im guessing that dirt got through the exhaust port then scrathced the bottom of the connecting rod and then it eventually made a litlle gouge on the piston.......not big enough for it to blow the engine but just enough for it to blow glow plugs and idle funny
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#28
sorry bud, but thats impossible lol
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#29
I really doubt that it came thru the exhaust. It looks like you have alot of scrap on top of your piston.
Tekno EB48.4 HobbyWing XR8 Sanwa M12
Reply
#30
Judging by the piston, there is a slight bit of detonation or pitting on the edges, prolly from the low deck height. The bead blasted look on top is from running lean. If i get a chance I will show you what the top one of my pistons loooks like
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#31
ok....well im sending it into traxxas so hopefully theyll fix it......but it was only at 290 for a few seconds and still had plenty of smoke coming out
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#32
you may have been lean bottom rich top, or rich bottom lean top, and not have even know it. I am betting it was the second case.
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#33
That piston shows signs of running lean, I disassembled my 3.3 the other day and had a dark brown maple syrup color going.
Mugen MBX5T
RBS5
RB2045
Futaba 3PM
Hitec 5955, 5965
Reply
#34
ok.......well its weird cause becuase i went to hte track on tuesday I had a brown maple syrup like color ring and the rest was good.....i must have run too lean at the track and thats why it was blowing glow plugs.......how do i know if im too lean then?
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#35
well it wasn't cutting out, and the temps were good so.....
8ight | Mini-T | CEN Boat | Stampede | JR R-1

ALL RC STUFF FOR SALE. PM FOR DETAILS.
Reply
#36
you know what....my temp gun was prolly off, becuase remember when it was sizzling kyle??

my temp gun was prolly off.

it wont start cutting out till it hits about 320-330
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#37
thatll do it, did u go to LH? those long ass straights. Did u re tune when u got there, i would recommend opening ur HSN about 4-5 hours before even hitting the track
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#38
Also, check and make sure your airfilter ain't dirty.
Tekno EB48.4 HobbyWing XR8 Sanwa M12
Reply
#39
well the motor is shipped off to traxxas........they will hopefully figure out whats wrong with it.......oh and I just checked my temp gun, it works good now.

maybe it got screwed up when i dropped it 20 feet onto rocks cause travis didnt catch it.

I dont think my temps are what are causing me to blow glow plugs, its something else.
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#40
traxxas thrasher Wrote:maybe it got screwed up when i dropped it 20 feet onto rocks cause travis didnt catch it.
.

What?!!!!?? Were you up on the driver's stand or something?!??!?!
Tekno EB48.4 HobbyWing XR8 Sanwa M12
Reply
#41
The long strait isn't any different than running through a field or in the street out in front of your house.

If it was sizzling it was over 320F, probably around 400F. Also motors don't have to be at a certain temp before they start cutting out. They cut out because of lack of gas, not being to hot. If your too lean your engine could cut out even when you first start it, while the motor is still cold.

The "cutting out" is due to no fuel in the crank case, IE, too lean.

I know you said it wasn't cutting out and you saw smoke but it was definitely too lean bro, motor might be shot.....
Mugen MBX5T
RBS5
RB2045
Futaba 3PM
Hitec 5955, 5965
Reply
#42
dang.......well how do i tell if its not too lean then??

matt yeah i was on top of the drivers stand and threw it down to travis and he missed it.

maybe that impact screwed it up enuogh for a few seconds and caused it to be too lean and the temps got to high and fried it
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#43
well when ur goin down the straight does it whine out quickly and then seem to slow down almost on its own toward the end of the straight, almost like it is dieing out? like Tex said no fuel man u scorched that puppy
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#44
u cant depend on temps sometimes, if its not running to its optimum performance than u need to re tune. sound is important, and also experience. You should be able to "feel" a difference in the motor when it is and is not tuned right
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#45
well i have never had this problem with any of my other engines.....it was going kinda slow down the straight cause of no traction so i leaned it uot a bit and it was a little faster.......I must have leaned it out too much and didnt hear it cause travis and kyle were driving with me
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#46
Hella clear pic dude! nice...

Sadly it does show some signs that there may be some big problems...

Was there and compression left in the engine or was it gettin loose??? How bout when it was warm? would it roll over easily then?
Dont mess wit my sig Line tune!
--Then follow the rules! haha!-- -Tune
Reply
#47
rocco all motors roll over easy when they are warm...lol
Here is a link to my website-
http://www.czech-it-out-graphics.com
1/29/07 never forget....TTT Confusedalute:
Bringing old know-it-all blow hards back to reallity at a forum near you

"Always Imitated, Never Duplicated"
Reply
#48
I think he means REALLY EASY. not just easy.......
Mugen MBX5T
RBS5
RB2045
Futaba 3PM
Hitec 5955, 5965
Reply
#49
nope it had plenty of compression. I dont understand hoe it could have been to lean.....I had soooooo much smoke comin out and the temps were mostly at 230-250

well i know i went down the back straight and my slipper clutch was super loose to weere i hadi t full throttle and it was barely moving.....could that explain the lean and why it had a rough top??
Losi 8ight with v-spec[SIZE="4"]
[/SIZE]
Reply
#50
that could have done it too, with the loose traction, the motor was revving higher, could have heated it up faster, and then when the slipper kept coming lose the same thing happened, hopefully traxxas will give you a new p/s
8ight | Mini-T | CEN Boat | Stampede | JR R-1

ALL RC STUFF FOR SALE. PM FOR DETAILS.
Reply


Possibly Related Threads…
Thread Author Replies Views Last Post
  trx 3.3 engine problem help please? gregk20 1 2,986 08-11-2010, 08:02 PM
Last Post: Traxxas_Junkee
  question about a vspec engine eraser 83 17,431 02-06-2008, 04:36 PM
Last Post: J-Dub
  Cold weather engine tune rcrunr1 5 2,985 01-25-2008, 06:15 PM
Last Post: J-Dub
  cleaning engine internals AddictedtoNITRO 26 7,909 12-26-2007, 01:25 AM
Last Post: J-Dub
  Comprehensive engine dyno results mikeh 14 18,143 10-31-2007, 02:31 PM
Last Post: Czech-it-Out Graphics
  nitro tc3 engine suggestion hotrodlincoln 5 2,952 09-11-2007, 01:16 PM
Last Post: Tex
  Learning engine mods cr4sh_27 21 6,246 08-12-2007, 02:07 AM
Last Post: Thirdgen89GTA
  Big Block Revo Problems? No More! :D J-Dub 12 4,429 07-25-2007, 06:02 PM
Last Post: J-Dub
  Mugen engine? motoxer4life 60 12,689 07-11-2007, 12:12 PM
Last Post: Czech-it-Out Graphics
  engine/esc combo? AddictedtoNITRO 3 2,526 06-24-2007, 08:40 PM
Last Post: AddictedtoNITRO

Forum Jump:


Users browsing this thread: 9 Guest(s)